Liner O-ring failure |
02-27-2024, (Subject: Liner O-ring failure ) Post: #13 | |||
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RE: Liner O-ring failure Thought I should give an update on this engine, I rebuilt the engine myself with all genuine OEM parts, new head, reman rods, counter bores cut and shimmed to .015, and all the other extra steps mentioned, had a massive rail leak and narrowed down to number two injector, replaced injector and only lost couple hundred PSI in a minute, truck has been running great ever since and just did the 50,000 mile break in overhead adjustment, also with careful driving fuel mileage is above average for the type of work I do, thanks for the pointers and advice I was given! | |||
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Messages In This Thread |
Liner O-ring failure - Truckdriven - 06-19-2023, RE: Liner O-ring failure - tree98 - 06-19-2023, RE: Liner O-ring failure - Truckdriven - 06-19-2023, RE: Liner O-ring failure - Mr Hagg - 06-19-2023, RE: Liner O-ring failure - Rawze - 06-19-2023, RE: Liner O-ring failure - Truckdriven - 06-19-2023, RE: Liner O-ring failure - Truckdriven - 06-19-2023, RE: Liner O-ring failure - Truckdriven - 06-19-2023, RE: Liner O-ring failure - Truckdriven - 06-19-2023, RE: Liner O-ring failure - Rawze - 06-20-2023, RE: Liner O-ring failure - Truckdriven - 06-20-2023, RE: Liner O-ring failure - Rawze - 06-20-2023, RE: Liner O-ring failure - Truckdriven - 02-27-2024 RE: Liner O-ring failure - tree98 - 02-27-2024, |
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