Rawze.com: Rawze's ISX Technical Discussion and more
Injector return flow test - Printable Version

+- Rawze.com: Rawze's ISX Technical Discussion and more (http://rawze.com/forums)
+-- Forum: Big Truck Technical Discussion... (/forumdisplay.php?fid=1)
+--- Forum: ISX Related Help (/forumdisplay.php?fid=68)
+--- Thread: Injector return flow test (/showthread.php?tid=3998)

Pages: 1 2


Injector return flow test - CANNONBALL - 01-12-2019

quickserve says 200ml. Breaks Down 6.78 oz. marks on the bottles are 1/2 so 8.45 oz.

Run the injector kill test and try to let it run on 1 hole. 1, 2, 3, 4 it tries to die. It’ll run on 5 or 6 all day long just 1 hole.

Are the front 4 injectors all bad?


RE: Injector return flow test - snailexpress - 01-12-2019

(01-12-2019 )CANNONBALL Wrote:  quickserve says 200ml. Breaks Down 6.78 oz. marks on the bottles are 1/2 so 8.45 oz.

Run the injector kill test and try to let it run on 1 hole. 1, 2, 3, 4 it tries to die. It’ll run on 5 or 6 all day long just 1 hole.

Are the front 4 injectors all bad?
It's possible at least to say. Run this test a few times to have consistent measurement.


RE: Injector return flow test - CANNONBALL - 01-12-2019

The truck did get a bad batch of fuel. Had to change filters 9 times within a 10k mile interval to get it cleaned out.


RE: Injector return flow test - barf - 01-12-2019

I never heard of the injector return flow test so I probably have no idea what I'm talking about.

Any chance #4 is bad and the front 3 is something else like the metering valve?


RE: Injector return flow test - CANNONBALL - 01-13-2019

It’s a 2350.


RE: Injector return flow test - CANNONBALL - 01-13-2019

Guess I should’ve said one side of the high pressure fuel pump head was bad along with the check valve in the head letting fuel leak off. New head fixed part of the problem but still having issues.


RE: Injector return flow test - snailexpress - 01-13-2019

(01-13-2019 )CANNONBALL Wrote:  Guess I should’ve said one side of the high pressure fuel pump head was bad along with the check valve in the head letting fuel leak off. New head fixed part of the problem but still having issues.
Could you take video for gear pump return line test. How much air bubbles is in return fuel?.


RE: Injector return flow test - Signature620 - 01-13-2019

Re-tension all the high pressure connectors and run the test again.


RE: Injector return flow test - Unilevers - 01-13-2019

(01-13-2019 )CANNONBALL Wrote:  Guess I should’ve said one side of the high pressure fuel pump head was bad along with the check valve in the head letting fuel leak off. New head fixed part of the problem but still having issues.


chances are when the pump went it ate 1-4. If it were my truck personally and i had that many down it would get a 6 pack of injectors.

Im with signature, tighten the high pressure connectors and run it a few more times but i doubt thats it as it can and should be able to run on 1-4 by themselves.